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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-05812MCLAUGHLIN, A C
32
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
11/17/2021
RANGELY
72370
RIO BLANCO  103
SWNE 13 2N103W 6
314486View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:9/19/2011MIT Assigned By:KOEHLER, BOB
Date Recv'd:9/22/2011Facility ID: 150200
DocNum:1771506Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON USA INC
Address:100 CHEVRON ROAD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameMCLAUGHLIN, A C
Operator contact:DIANE L.  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:CASING LEAK
Repair Desc:UIC REPAIR - RUN LINER
Test Date:9/16/2011
Field Rep:
Approved Date:2/22/2012
Approved by:KOEHLER, BOB
Last Approved MIT:5/11/2007
Injection/Producing Formation Zones:WEBR
Perforation Interval:NA
Open Hole Interval:6350-6480
Bridge/Cement Plug Depth:NA
Tubing Size:2.875
Tubing Depth:6292
Top Packer Depth:6111
Multiple Packers:Y
 
Condition of approval:
New Form 5 was submitted and approved. NOAV was cleared with No Action, repair and MIT-retest completed on time. BK cleared out NOAV for Chuck Browning.
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE
5 MIN CASE
CASE BEFORE
FINAL CASE810
FINAL TUBE
INITIAL TUBE
LOSS OR GAIN0
START CASE810
Channel TestTest Date
CBL 9/9/2011