Form 21 | Related Doc | Date Submitted: | 9/19/2011 | MIT Assigned By: | KOEHLER, BOB | Date Recv'd: | 9/22/2011 | Facility ID: | 150200 | DocNum: | 1771506 | Facility Status: | AC | Operator Information: | Oper. No. | 16700 | Operator: | CHEVRON USA INC | Address: | 100 CHEVRON ROAD RANGELY CO 81648 | Type Of Facility: | UIC ENHANCED RECOVERY | Well Status: AC | Facility Name | MCLAUGHLIN, A C | Operator contact: | DIANE L. PETERSON | Location: | | qtrqtr: SENE | section: 16 | township: 2N | range: 103W | meridian: 6 |
| MIT Details: | Test Type: | VERIFICATION OF REPAIRS | Repair Type: | CASING LEAK | Repair Desc: | UIC REPAIR - RUN LINER | Test Date: | 9/16/2011 | Field Rep: | | Approved Date: | 2/22/2012 | Approved by: | KOEHLER, BOB | Last Approved MIT: | 5/11/2007 | Injection/Producing Formation Zones: | WEBR | Perforation Interval: | NA | Open Hole Interval: | 6350-6480 | Bridge/Cement Plug Depth: | NA | Tubing Size: | 2.875 | Tubing Depth: | 6292 | Top Packer Depth: | 6111 | Multiple Packers: | Y | | Condition of approval: | New Form 5 was submitted and approved. NOAV was cleared with No Action, repair and MIT-retest completed on time. BK cleared out NOAV for Chuck Browning. | Test Data: | Wellbore Channel Test: | Reading Type | Pressure | 10 MIN CASE | | 5 MIN CASE | | CASE BEFORE | | FINAL CASE | 810 | FINAL TUBE | | INITIAL TUBE | | LOSS OR GAIN | 0 | START CASE | 810 |
| Channel Test | Test Date | CBL | 9/9/2011 |
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