Form 21 | Related Doc |
Date Submitted: | N/A | MIT Assigned By: | DILLON, DAVID |
Date Recv'd: | 6/8/2004 | Facility ID: | 150200 |
DocNum: | 1494143 | Facility Status: | AC |
Operator Information: |
Oper. No. | 16700 |
Operator: | CHEVRON U S A INC |
Address: | 6001 BOLLINGER CANYON RD SAN RAMON CA 94583 |
Type Of Facility: | UIC ENHANCED RECOVERY | Well Status: AC |
Facility Name | GRAY |
Operator contact: | |
Location: | | qtrqtr: SENE | section: 16 | township: 2N | range: 103W | meridian: 6 |
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MIT Details: |
Test Type: | VERIFICATION OF REPAIRS |
Repair Type: | TUBING/PACKER LEAK |
Repair Desc: | UIC Repair, fished model D packer, ran 5 1/2" liner from surface to 6123'. |
Test Date: | 6/2/2004 |
Field Rep: | |
Approved Date: | 1/25/2006 |
Approved by: | DILLON, DAVID |
Last Approved MIT: | 5/9/2002 |
Injection/Producing Formation Zones: | WEBR |
Perforation Interval: | 6264-6590 |
Open Hole Interval: | NA |
Bridge/Cement Plug Depth: | NA |
Tubing Size: | 2.875 |
Tubing Depth: | 6569 |
Top Packer Depth: | 6088 |
Multiple Packers: | Y |
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Condition of approval: |
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Test Data: | Wellbore Channel Test: | Reading Type | Pressure | 10 MIN CASE | | 5 MIN CASE | | CASE BEFORE | -1 | FINAL CASE | 815 | FINAL TUBE | -1 | INITIAL TUBE | -1 | LOSS OR GAIN | | START CASE | 800 |
| No channel test. |
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