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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-07689GRAY
A-17X
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
8/15/2014
RANGELY
72370
RIO BLANCO  103
SESE 13 2N103W 6
314984View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:N/AMIT Assigned By:DILLON, DAVID
Date Recv'd:6/8/2004Facility ID: 150200
DocNum:1494143Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON U S A INC
Address:6001 BOLLINGER CANYON RD  SAN RAMON  CA 94583
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameGRAY
Operator contact: 
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:UIC Repair, fished model D packer, ran 5 1/2" liner from surface to 6123'.
Test Date:6/2/2004
Field Rep:
Approved Date:1/25/2006
Approved by:DILLON, DAVID
Last Approved MIT:5/9/2002
Injection/Producing Formation Zones:WEBR
Perforation Interval:6264-6590
Open Hole Interval:NA
Bridge/Cement Plug Depth:NA
Tubing Size:2.875
Tubing Depth:6569
Top Packer Depth:6088
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE
5 MIN CASE
CASE BEFORE-1
FINAL CASE815
FINAL TUBE-1
INITIAL TUBE-1
LOSS OR GAIN
START CASE800
No channel test.