Skip to Main Content

Incident Search

COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-09187EMERALD
44AX
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
8/12/2022
RANGELY
72370
RIO BLANCO  103
SWNW 36 2N103W 6
315760View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:12/9/2014MIT Assigned By:Browning, Chuck
Date Recv'd:12/9/2014Facility ID: 150200
DocNum:1171745Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameEMERALD
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:OTHER
Repair Desc:FISHED PACKERS / USED PLASMA TOOL TO TREAT PERFS / RUN IN WITH 196 JTS NEW FIBERLINED TUBING AND PACKERS
Test Date:12/9/2014
Field Rep:Browning, Chuck
Approved Date:12/9/2014
Approved by:Browning, Chuck
Last Approved MIT:10/4/2012
Injection/Producing Formation Zones:WEBR
Perforation Interval:6456-6688
Open Hole Interval:NA
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6427.8
Top Packer Depth:6307.8
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1240
5 MIN CASE1230
CASE BEFORE0
FINAL CASE1240
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN20
START CASE1220
No channel test.