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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-01077COLTHARP W H
C-1
SCOUT ENERGY MANAGEMENT LLC
10779
AC
5/1/2023
RANGELY
72370
RIO BLANCO  103
SESW 36 2N102W 6
314275View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:11/19/2014MIT Assigned By:Browning, Chuck
Date Recv'd:11/19/2014Facility ID: 150200
DocNum:1171744Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameCOLTHARP W H
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:PULL TUBING AND PACKERS. rih W/ 165 JOINTS NEW TUBING 2 7/8" TUBING. RECEIVED PACKER DEPTH VARIANCE DOC# 400725028
Test Date:11/19/2014
Field Rep:Browning, Chuck
Approved Date:11/19/2014
Approved by:Browning, Chuck
Last Approved MIT:4/24/2012
Injection/Producing Formation Zones:WEBR
Perforation Interval:5836-6334
Open Hole Interval:NA
Bridge/Cement Plug Depth:NA
Tubing Size:2.875
Tubing Depth:5727.6
Top Packer Depth:5328
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1300
5 MIN CASE1305
CASE BEFORE0
FINAL CASE1300
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN-10
START CASE1310
No channel test.