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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-01075MCLAUGHLIN, A C
47X
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
10/18/2021
RANGELY
72370
RIO BLANCO  103
SWSW 23 2N103W 6
314273View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:9/24/2014MIT Assigned By:Browning, Chuck
Date Recv'd:9/24/2014Facility ID: 150200
DocNum:1171718Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameMCLAUGHLIN, A C
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:CASING LEAK
Repair Desc:RUN 5 1/2" 17# LINER FROM SURFACE TO 5980'. CORRECT VIOLATION DOCUMENT #668402005
Test Date:9/24/2014
Field Rep:Browning, Chuck
Approved Date:9/24/2014
Approved by:Browning, Chuck
Last Approved MIT:6/1/2009
Injection/Producing Formation Zones:WEBR
Perforation Interval:6160-6660
Open Hole Interval:NA
Bridge/Cement Plug Depth:NA
Tubing Size:2.875
Tubing Depth:6122.3
Top Packer Depth:5911
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE1225
5 MIN CASE1225
CASE BEFORE0
FINAL CASE1225
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN0
START CASE1225
No channel test.