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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-05795MCLAUGHLIN, A C
42
SCOUT ENERGY MANAGEMENT LLC
10779
AC
5/1/2023
RANGELY
72370
RIO BLANCO  103
NWSE 13 2N103W 6
314477View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:10/12/2011MIT Assigned By:BROWNING, CHUCK
Date Recv'd:11/4/2011Facility ID: 150200
DocNum:1171342Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameMCLAUGHLIN, A C
Operator contact:DIANE  PTERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:PULLED TBG AND FISHE PACKERS.CLEAN OUT WELLBORE. RUN 5 1/2" LNR FROM SFC TO 6038'. RUN CBL. RIH W/ 188 JTS FIBERLINED TBG & NEW PACKERS. TEST CSG. OK
Test Date:10/11/2011
Field Rep:
Approved Date:11/4/2011
Approved by:BROWNING, CHUCK
Last Approved MIT:9/30/2006
Injection/Producing Formation Zones:WEBR
Perforation Interval:6300-6395
Open Hole Interval:NA
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6248.9
Top Packer Depth:5980.8
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE820
5 MIN CASE820
CASE BEFORE0
FINAL CASE820
FINAL TUBE
INITIAL TUBE
LOSS OR GAIN0
START CASE820
Channel TestTest Date
CBL 10/5/2011