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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-05595EMERALD
34
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
4/21/2023
RANGELY
72370
RIO BLANCO  103
SESE 25 2N103W 6
314395View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:10/2/2007MIT Assigned By:KRABACHER, JAY
Date Recv'd:10/5/2007Facility ID: 150200
DocNum:1171016Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameEMERALD
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:OTHER
Repair Desc:well failed annual routine insp. "field specialist bled off surface gas and tested integrity. well passed."
Test Date:9/8/2007
Field Rep:
Approved Date:10/5/2007
Approved by:KRABACHER, JAY
Last Approved MIT:5/8/2006
Injection/Producing Formation Zones:WEBR
Perforation Interval:5614 - 6361
Open Hole Interval:NA
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6029
Top Packer Depth:5474
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE785
5 MIN CASE790
CASE BEFORE0
FINAL CASE785
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN-5
START CASE790
No channel test.