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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-06169FEE
59
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
5/30/2023
RANGELY
72370
RIO BLANCO  103
SESE 21 2N102W 6
311800View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:9/18/2007MIT Assigned By:KRABACHER, JAY
Date Recv'd:9/24/2007Facility ID: 150200
DocNum:1171011Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameFEE
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:REPLACE 177 jts. tubing & 7" packer
Test Date:9/14/2007
Field Rep:
Approved Date:9/24/2007
Approved by:KRABACHER, JAY
Last Approved MIT:5/9/2006
Injection/Producing Formation Zones:WEBR
Perforation Interval:6059 - 6472
Open Hole Interval:NA
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6016
Top Packer Depth:5773
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE805
5 MIN CASE805
CASE BEFORE0
FINAL CASE805
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN0
START CASE805
No channel test.