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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-08028FEE
112X
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
4/30/2024
RANGELY
72370
RIO BLANCO  103
NWSE 19 2N102W 6
315174View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:7/24/2007MIT Assigned By:KRABACHER, JAY
Date Recv'd:7/30/2007Facility ID: 150200
DocNum:1170989Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameFEE
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:replace tbg w/180 jts.
Test Date:7/17/2007
Field Rep:
Approved Date:7/30/2007
Approved by:KRABACHER, JAY
Last Approved MIT:5/9/2006
Injection/Producing Formation Zones:WEBR
Perforation Interval:5844 - 6531
Open Hole Interval:NA
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:5700
Top Packer Depth:5614
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE820
5 MIN CASE820
CASE BEFORE0
FINAL CASE820
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN0
START CASE820
No channel test.