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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-06258RAVEN
A-4
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
5/31/2022
RANGELY
72370
RIO BLANCO  103
SWNE 31 2N102W 6
396937View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:4/25/2006MIT Assigned By:KRABACHER, JAY
Date Recv'd:4/28/2006Facility ID: 150200
DocNum:1170817Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameRAVEN
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:fish parted tubing, clean and replace 171 jts. new tubing
Test Date:4/22/2006
Field Rep:
Approved Date:4/28/2006
Approved by:KRABACHER, JAY
Last Approved MIT:5/4/2004
Injection/Producing Formation Zones:WEBR
Perforation Interval:5653 - 5664
Open Hole Interval:5686 - 6291
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:5603
Top Packer Depth:5517
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE800
5 MIN CASE800
CASE BEFORE0
FINAL CASE800
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN0
START CASE800
No channel test.