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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-06247FEE
44
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
12/1/2019
RANGELY
72370
RIO BLANCO  103
SESE 30 2N102W 6
314630View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:12/15/2005MIT Assigned By:KRABACHER, JAY
Date Recv'd:12/27/2005Facility ID: 150200
DocNum:1170798Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameFEE
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:replace 171 jts tubing
Test Date:12/14/2005
Field Rep:
Approved Date:12/27/2005
Approved by:KRABACHER, JAY
Last Approved MIT:5/24/2000
Injection/Producing Formation Zones:WEBR
Perforation Interval:5666 - 6224
Open Hole Interval:NA
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:5409
Top Packer Depth:5335
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE800
5 MIN CASE800
CASE BEFORE0
FINAL CASE800
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN0
START CASE800
No channel test.