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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-07978LACY, S B
7X
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
8/1/2023
RANGELY
72370
RIO BLANCO  103
NWSW 24 2N103W 6
315138View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:9/26/2005MIT Assigned By:KRABACHER, JAY
Date Recv'd:10/4/2005Facility ID: 150200
DocNum:1170786Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameLACY, S B
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:CASING LEAK
Repair Desc:repair csg leak @ 4197 - 4227. ran 189 jts of fiberline tbg
Test Date:9/23/2005
Field Rep:
Approved Date:10/4/2005
Approved by:KRABACHER, JAY
Last Approved MIT:8/5/2005
Injection/Producing Formation Zones:WEBR
Perforation Interval:5960 - 6580
Open Hole Interval:NA
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6342
Top Packer Depth:5820
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE750
5 MIN CASE750
CASE BEFORE0
FINAL CASE750
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN0
START CASE750
No channel test.