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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-05661EMERALD
9
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
7/2/2021
RANGELY
72370
RIO BLANCO  103
SWNE 26 2N103W 6
314416View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:12/30/2004MIT Assigned By:KRABACHER, JAY
Date Recv'd:4/22/2005Facility ID: 150200
DocNum:1170688Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON U S A INC
Address:6001 BOLLINGER CANYON RD  SAN RAMON  CA 94583
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameEMERALD
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:OTHER
Repair Desc:replace 182 jts of tubing with new fiberlined. cement squeeze casing leaks
Test Date:12/23/2004
Field Rep:
Approved Date:4/22/2005
Approved by:KRABACHER, JAY
Last Approved MIT:5/4/2004
Injection/Producing Formation Zones:WEBR
Perforation Interval:5998 - 6629
Open Hole Interval:NA
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:5793
Top Packer Depth:5715
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE800
5 MIN CASE800
CASE BEFORE0
FINAL CASE800
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN0
START CASE800
No channel test.