Skip to Main Content

Incident Search

COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-06112FEE
24
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
4/1/2017
RANGELY
72370
RIO BLANCO  103
NWSW 17 2N102W 6
336556View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:9/3/2004MIT Assigned By:KRABACHER, JAY
Date Recv'd:10/8/2004Facility ID: 150200
DocNum:1170668Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON PRODUCTION COMPANY
Address:100 CHEVRON RD  RANGELY  CO 81648
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameFEE
Operator contact:DIANE  PETERSON
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:replaced 180 jts. tubing
Test Date:9/1/2004
Field Rep:
Approved Date:10/8/2004
Approved by:KRABACHER, JAY
Last Approved MIT:6/12/2002
Injection/Producing Formation Zones:WEBR
Perforation Interval:6247 - 6500
Open Hole Interval:NA
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:5917
Top Packer Depth:5760
Multiple Packers:N
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE795
5 MIN CASE800
CASE BEFORE0
FINAL CASE790
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN-10
START CASE800
Channel TestTest Date
TRACER SURVEY 11/22/2002