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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-07191CARNEY UNIT
2X
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
12/1/2019
RANGELY
72370
RIO BLANCO  103
NENE 4 1N102W 6
314772View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:12/9/1999MIT Assigned By:ADKINS, JAIME
Date Recv'd:4/29/2003Facility ID: 150200
DocNum:1093018Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON U S A INC
Address:P O BOX 4791  HOUSTON  TX 77210-4791
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameCARNEY UNIT
Operator contact: 
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:CASING LEAK
Repair Desc:RAN LINER
Test Date:12/6/1999
Field Rep:
Approved Date:2/16/2000
Approved by:ADKINS, JAIME
Last Approved MIT:5/27/1997
Injection/Producing Formation Zones:WEBR
Perforation Interval:5625-6382
Open Hole Interval:NA
Bridge/Cement Plug Depth:NA
Tubing Size:2.875
Tubing Depth:6108
Top Packer Depth:5558
Multiple Packers:N
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE825
5 MIN CASE830
CASE BEFORE
FINAL CASE825
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN-5
START CASE830
No channel test.