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COGIS - Mechanical Integrity Test Report
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation IDRelated Facilities
WELL05-103-05595EMERALD
34
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
4/21/2023
RANGELY
72370
RIO BLANCO  103
SESE 25 2N103W 6
314395View Related Related
 
Form 21View Related Related View DocsDoc
Date Submitted:7/3/2001MIT Assigned By:BELL, MORRIS
Date Recv'd:4/14/2003Facility ID: 150200
DocNum:1069322Facility Status:AC
Operator Information:
Oper. No.16700
Operator:CHEVRON U S A INC
Address:P O BOX 4791  HOUSTON  TX 77210-4791
Type Of Facility:UIC ENHANCED RECOVERYWell Status: AC
Facility NameEMERALD
Operator contact: 
Location:  qtrqtr: SENE section: 16 township: 2N range: 103W meridian: 6
MIT Details:
Test Type:VERIFICATION OF REPAIRS
Repair Type:TUBING/PACKER LEAK
Repair Desc:
Test Date:5/25/2001
Field Rep:
Approved Date:7/31/2001
Approved by:BELL, MORRIS
Last Approved MIT:11/16/1998
Injection/Producing Formation Zones:WEBR
Perforation Interval:5614 - 6361
Open Hole Interval:NA
Bridge/Cement Plug Depth:
Tubing Size:2.875
Tubing Depth:6030
Top Packer Depth:5475
Multiple Packers:Y
 
Condition of approval:
Test Data:Wellbore Channel Test:
Reading TypePressure
10 MIN CASE785
5 MIN CASE785
CASE BEFORE0
FINAL CASE800
FINAL TUBE0
INITIAL TUBE0
LOSS OR GAIN-15
START CASE785
No channel test.