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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-51779George
09N
PDC ENERGY INC
69175
PR
12/1/2024
WATTENBERG
90750
WELD  123
SWNE 21 4N64W 6
482391
   
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County Code: Sequence Code:
 
Surface Casing Depth: 1970 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
404476812Form 1712/8/202512/17/2025FLOWING0NO FLOW NONE0 NO FLOW 66No---- 
Click for SpecificsFull5/30/20256/9/2025 3Continuous--0No Flow88NoNoNo Annual Test.  3 PSI blew down to 0 PSI within first few seconds of test.  No pressure or flow observed for the remainder of the test. Operator will monitor pressure and re-test according to bradenhead policy.
404044174Form 1712/12/202412/31/2024FLOWING63CONTINUOUS WATER AND GAS0 WHISPER 2930No----Post-Production within 60 days of first sales. 63 PSI blew down to 0 PSI in 30 minutes. Whisper gas and water trickle observed throughout entire test. PDC will schedule a sampling event and submit results via form 43. PDC will monitor pressure and re-test according to bradenhead policy.
Click for SpecificsFull6/17/20246/25/2024 0No Flow--0No Flow00NoNoNoInitial Test Post Rig Release.  0 PSI, no pressure or flow observed for the entire 30 min test. PDC will monitor pressure and re-test according to bradenhead policy.