Skip to Main Content

Incident Search

 
BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-49586Huron
1N
PDC ENERGY INC
69175
PR
8/1/2025
WATTENBERG
90750
WELD  123
SESE 22 5N64W 6
437599
   
Search for Different Bradenhead:
County Code: Sequence Code:
 
Surface Casing Depth: 1691 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
Click for SpecificsFull4/22/20264/27/2026 0No Flow--0No Flow475422NoNoNoAnnual Test.  0 PSI, with no pressure or flow observed for the entire 30-minute test.  Operator will monitor pressure and re-test according to bradenhead policy.
404292362Form 177/9/20257/24/2025PLUNGER LIFT0NO FLOW NONE0 NO FLOW 588587No----Remediation follow up test. 0 PSI, no pressure or flow observed. Operator will monitor pressure and re-test according to bradenhead policy.
Click for SpecificsFull7/19/20247/29/2024 0No Flow--0No Flow649649NoNoNoAnnual Test.  0 PSI, with no pressure or flow observed for the entire 30-minute test.  PDC will monitor pressure and re-test according to bradenhead policy.
403620206Form 1712/7/202312/11/2023FLOWING0DOWN TO 0 GAS0 NO FLOW 730724No----Abatement system follow up test. 0 PSI, no pressure or flow observed. PDC will monitor pressure and re-test according to bradenhead policy.
403387176Form 174/26/20234/27/2023FLOWING52CONTINUOUS WATER AND GAS0 NO FLOW 10251023Yes----Automation Alert test. 52 PSI water and gas flow blew down to 0 PSI in 5 minutes. No flow or pressure for the remainder of the test. PDC will monitor pressure and re-test according to bradenhead policy.
403149180Form 178/25/20228/29/2022FLOWING0DOWN TO 0 GAS0 NO FLOW 22882289No----Post Production test within 60 days of first sales, 0 PSI no pressure or flow observed for the entire test. PDC will monitor bradenhead pressure monthly and submit annual test.
403052613Form 175/17/20225/18/2022SHUT-IN0NO FLOW --0 NO FLOW 00No----Delayed Completions Test. 0 PSI, no pressure or flow observed for the entire test.
402983746Form 173/14/20223/14/2022SHUT-IN5NO FLOW --0 NO FLOW 00No----Delayed Completions Test, 5 PSI blew down to 0 PSI in 5 minutes. No pressure or flow observed for the remainder of the test.
402819964Form 178/23/20219/22/2021SHUT-IN173CONTINUOUS GAS0 NO FLOW 00YesYes--Duc Test 173 PSI gas flow, blew down to 0 PSI within first minute of test. No pressure or flow observed for the remainder of the test. PDC has collected a sample from this test and results will be submitted as soon as possible. PDC has scheduled another sampling event scheduled for september 30th.
402720916Form 176/14/20216/16/2021 255NO FLOW NONE0 NO FLOW 00Yes----Delayed Completions Test, 0 PSI no pressure or flow observed for the entire 30 minute test. This well is currently on abatement system to mitigate bradenhead pressure.
402765800Form 173/31/20217/30/2021SHUT-IN0NO FLOW --0  00No----Delayed Completions Test, 0 PSI No pressure or flow observed for the entire test.