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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-44984Raindance FD
20-322HN
PDC ENERGY INC
69175
PR
8/1/2024
WATTENBERG
90750
WINDSOR/WELD  123
NENE 30 6N67W 6
427917
   
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Surface Casing Depth: 1557 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
404008479Form 1711/25/202411/26/2024PLUNGER LIFT12WHISPER GAS0 NO FLOW 341341No----Remediation follow up test. 12 PSI whisper blew down to 0 PSI within first five minutes of test. No pressure or flow observed for the remainder of the test. PDC will monitor pressure and re-test according to bradenhead policy.
403799284Form 175/14/20245/21/2024SHUT-IN26CONTINUOUS WATER AND GAS0 WHISPER 00No----Annual test. 26 PSI cloudy water and gas flow blew down to 0 PSI in seconds, whisper gas and fluid trickle for entire test, ~2.5 gallons total. PDC will monitor pressure and re-test according to bradenhead policy.
403280481Form 171/4/20231/5/2023SHUT-IN0DOWN TO 0 GAS0 NO FLOW 200200No----Abatement system follow up test. 0 PSI, no pressure or flow observed. PDC will submit sundry with bradenhead details if needed as soon as possible. PDC will continue to monitor monthly.
403051736Form 175/12/20225/17/2022FLOWING297DOWN TO 0 WATER H200 NO FLOW 350342Yes--YesFailed retest. Water on open. Collected 1000mL sample. Flow died to trickle/drip. Produced about 1.5 gal total.
402870039Form 1711/3/202111/12/2021FLOWING439CONTINUOUS WATER H200 CONTINUOUS 370370YesNoYesTest per NTO. Water at open. Water for entire test. Made 3 gallons total.
402548556Form 1712/1/202012/8/2020FLOWING8CONTINUOUS WATER H200 CONTINUOUS 408408YesNoYesTest per NTO. Water drips for entire test. Made 3/4 of a gallon total.
402239563Form 1711/7/201911/14/2019FLOWING22DOWN TO 0 --0 NO FLOW 942948No----Test after DOFP. Delay due to continuous surface operations. Produced 1 cup of water on open then died < 10 secs.
401989659Form 173/28/20193/29/2019SHUT-IN34NO FLOW --0 NO FLOW 00No----Test before frac. Bled down in 5 seconds.
401668434Form 176/1/20186/8/2018SHUT-IN200CONTINUOUS --0 WHISPER 00No----Second test, six months after rig release. Blew down to continuous in 10 seconds. Well not completed.
401458656Form 1711/13/201711/15/2017SHUT-IN370DOWN TO 0 --1 NO FLOW 00No----