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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-44317BUTTERBALL
24N2-34HZ
KERR MCGEE OIL & GAS ONSHORE LP
47120
PR
2/4/2018
WATTENBERG
90750
WELD  123
NENE 10 2N67W 6
319164
   
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Surface Casing Depth: 1853 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
Click for SpecificsFull9/15/202510/7/2025 0No FlowNone0No Flow281281NoNN Surface Casing produced no liquid.
Click for SpecificsFull7/17/20248/20/2024 0No FlowNone--No Flow382382NoNN Surface Casing produced no liquid.
Click for SpecificsFull9/7/202310/16/2023Plunger Lift0No FlowNone--No Flow384384NoNN Surface Casing produced no liquid.
Click for SpecificsFull10/5/202211/8/2022Plunger Lift0No FlowNone--No Flow364364NoNN Surface Casing produced no liquid.
Click for SpecificsFull7/7/20218/23/2021Plunger Lift0No FlowNone--No Flow450450NoNN Surface Casing produced no liquid.
402502182Form 1710/1/202010/2/2020 5CONTINUOUS --0 NO FLOW 527502No----Surface Casing produced no liquid.
402119237Form 176/28/20197/23/2019PLUNGER LIFT57GAS --1 WHISPER 822821No----Surface casing produced no fluids. 15 minute shut in results in 25 psi. 30 minute blow down results in whisper.
401573369Form 173/8/20183/14/2018PLUNGER LIFT26GAS --0 DOWN TO 0 18181794No----Surface casing produced no fluids. Surface casing shut in for 15 min ended with a whisper. Well and master shut in. Post turn on to sales Form 17.
401372611Form 178/9/20178/10/2017 483CONTINUOUS --1 WHISPER 11No----SURFACE CASING PRODUCED MUD. BLEW DOWN SURFACE CASING AN EXTRA 30 MIN ENDED WITH A WHISPER. SHUT IN SURFACE CASING FOR 15 MIN ENDED WITH 55 PSI.