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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-37670HENRICKSON FEDERAL
36C-18HZ
KERR MCGEE OIL & GAS ONSHORE LP
47120
PR
6/10/2014
WATTENBERG
90750
WELD  123
NESW 7 3N66W 6
330278
   
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Surface Casing Depth: 1017 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
Click for SpecificsFull6/24/202410/28/2024 2ContinuousNone--No Flow200202NoNN Surface Casing produced no liquid.
Click for SpecificsFull8/17/20239/11/2023Plunger Lift1WhisperNone--No Flow229230NoNN Surface Casing produced no liquid.
403075806Form 175/31/20226/10/2022 1WHISPER GAS0 NO FLOW 197205No----Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull6/15/20217/19/2021Plunger Lift2ContinuousNone--No Flow241240NoNN Surface Casing produced no liquid.
Click for SpecificsFull10/29/202012/21/2020Plunger Lift1CONTINUOUS ----DOWN TO 0 326330NoNoNo Surface Casing produced no liquid.
Click for SpecificsFull12/2/201912/10/2019 1Whisper (Very Low Flow) 0Down To Zero282283NoNoNoSurface casing produced no liquid.
400959057Form 1711/20/201512/22/2015 1GAS --0 DOWN TO 0 830837No----END OF 30 DAY TEST AND AFTER SC WAS SHUT IN FOR 7 DAYS. SC PRODUCED NO FLUIDS DURING TEST. SHUT IN SC FOR 15 MIN ENDED WITH ZERO PSI.
400931736Form 1710/9/201511/5/2015 26GAS --0 DOWN TO 0 869870No----SC DID NOT PRODUCE ANY FLUID. 15 MIN BUILD UP. WHISPER.
400986309Form 174/10/20142/9/2016PLUNGER LIFT39GAS -->0 DOWN TO 0 ----No----CASING INACCESSIBLE---SC produced no fluid during form 17 test. Did not shut in well during test.