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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-31531STROHAUER F
32-21D
PDC ENERGY INC
69175
PA
5/10/2024
WATTENBERG
90750
WELD  123
NWSE 32 5N65W 6
417001
   
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Surface Casing Depth: 563 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
403673915Form 171/31/20242/1/2024SHUT-IN132CONTINUOUS GAS52 CONTINUOUS 00No----Annual test. 132 PSI strong gas for entire test, fluid started at 20 minute mark and continued for the remainder of the test. Pressure only reduced to 52 PSI in 30 minutes. Most recent sample from 10/2023. PDC will monitor pressure and re-test according to bradenhead policy.
403607631Form 1711/27/202311/28/2023SHUT-IN40CONTINUOUS GAS0 NO FLOW 520520No----Pre-P&A. 40 PSI blew down to 0 PSI within first 10 minutes of test. No pressure or flow observed for the remainder of the test. PDC collected a sample 10/2023.
403548067Form 179/28/202310/3/2023SHUT-IN14CONTINUOUS GAS0 WHISPER 215215Yes----Pre-P&A. 14 PSI whisper gas blew down to 0 PSI in 30 minutes. Fluid present from 22 minute mark lasting 2 minutes. PDC will schedule a sampling event and submit results via form 43.
403282901Form 171/5/20231/9/2023SHUT-IN120CONTINUOUS GAS20 CONTINUOUS 775775Yes----Annual Test. 120 PSI blew down to 20 PSI in 30 minutes. Hard gas from start until 15 minute mark then whisper gas for remainder of test. Water began at 25 minute mark as well and continued for remainder of test. PDC will schedule a sampling event and submit results via form 43 as well as a remediation plan via sundry as soon as possible. PDC will continue to monitor monthly.
403053995Form 175/18/20225/19/2022SHUT-IN56CONTINUOUS GAS36 CONTINUOUS 775775No----Monthly Gauge High Pressure Follow-Up, 56 PSI gas flow blew down to 36 PSI in 30 minutes. Gas flow present for the duration of the test, water flow began at 10 minutes and lasted the remainder of the test. Sample collected 4/12/2022. PDC will continue to monitor monthly. See doc# 402971952 for Wellbore Diagram.
402971946Form 173/2/20223/3/2022SHUT-IN0NO FLOW --0 NO FLOW 00No----Abatement system follow up test. No pressure or flow observed. PDC will submit sundry with bradenhead details if needed as soon as possible. PDC will continue to monitor monthly.
402865470Form 178/16/202111/9/2021SHUT-IN100WHISPER GAS AND VAPOR5 WHISPER 77Yes----Post-production, 100 PSI whisper gas and vapor blew down to 5 PSI in thirty minutes. PDC will submit sundry with bradenhead details as soon as possible. PDC will schedule a sampling event and submit results via form 43.
402719661Form 173/3/20216/15/2021SHUT-IN12NO FLOW --0  00No----Abatement system follow up test. No pressure or flow observed. PDC will submit sundry with bradenhead details as soon as possible.
402456986Form 177/30/20207/30/2020SHUT-IN80GAS --0 NO FLOW 00No----Annual Test, 80 PSI blew down to 0 PSI within first min of test. No pressure or flow observed for the remainder of test. PDC will attempt to collect a sample and submit a remeidation sundry.
402242407Form 1711/8/201911/18/2019PLUNGER LIFT250GAS --130 GAS 685685YesYes--Annual bradenhead testing. Bradenhead flowed gas, no fluid. Bradenhead will be sampled and results to be uploaded into EDD when available.