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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-29340MOSER
17-21
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
2/1/2018
WATTENBERG
90750
WELD  123
NWNE 21 3N65W 6
336444
   
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Surface Casing Depth: 742 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
401368077Form 178/3/20178/7/2017 225GAS --1 WHISPER 10821084YesYes--SURFACE CASING PRODUCED NO FLUIDS. BLEW DOWN SURFACE CASING AN EXTRA 30 MIN. ENDED WITH A WHISPER. SHUT IN SURFACE CASING FOR 15 MIN ENDED WITH 6 PSI. WELL AND MASTER SHUT IN.
400852042Form 176/1/20156/11/2015PLUNGER LIFT102GAS --0 DOWN TO 0 10881090No----SC PRODUCED NO FLUID. INITIAL TEST ON 5-27-15 SHOWED 148 PSI WITH GAS AND WATER. DURING THE TEST 1 GALLON OF WATER WAS PRODUCED. AFTER 30 MINS THE SC WAS STILL WHISPERING AND BUBBLING WATER.
400836111Form 174/21/20155/6/2015PLUNGER LIFT113GAS --1 GAS 997999No----SURFACE CASING PRODUCED 35 GALLONS OF WATER DURING FORM 17 TEST. MONITORED THE SURFACE CASING AN EXTRA 30 MINUTES, PRESSURE STAYED AT A WHISPER OF GAS. SHUT THE SURFACE CASING IN FOR 15 MINUTES, PRESSURE BUILT UP TO 5 PSI. POST REMEDIATION BLOW-DOWN ON 4-9-2015, PRESSURE AT 183 PSI, AND BLEW-DOWN TO A WHISPER.
400730897Form 1710/9/201411/13/2014PLUNGER LIFT263GAS --105 GAS 513515No----SC PRODUCED NO FLUIDS, MONITORED AN EXTRA 30 MINS, ENDED WITH 50 PSI, SHUT IN SC FOR 15 MIN, PRESSURE BUILT UP TO 73 PSI
400367727Form 1712/10/20121/10/2013PLUNGER LIFT175GAS --<1 GAS 310319No----Surface casing produced no fluid during the form 17 test.