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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-26783MEGAN H
16-33
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
4/12/2023
WATTENBERG
90750
WELD  123
SWSW 16 3N65W 6
310674
   
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Surface Casing Depth: 635 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
403302551Form 171/25/20231/26/2023 0NO FLOW NONE0 NO FLOW 11511151No---- Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull2/8/20223/14/2022Plunger Lift1WhisperNone--No Flow10041002NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull2/25/20213/15/2021Plunger Lift1WhisperNone--No Flow11151115NoNoNo Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull1/15/20206/8/2020 1Whisper (Very Low Flow) 0Down To Zero10591061NoNoNoTubing shut in. Surface casing produced no liquid.
Click for SpecificsFull2/27/201912/10/2019 1Whisper (Very Low Flow) 0Down To Zero10231023NoNoNoTubing shut in. Surface casing produced no liquid.
400962639Form 1712/16/201512/31/2015 1GAS --0 DOWN TO 0 850850No----SC PRODUCED NO FLUIDS DURING TEST. SHUT IN SC FOR 15 MIN ENDED WITH ZERO PSI. POST REMEDIATION TEST BLEW DOWN SC ON 12-3-15 WITH A WHISPER OF GAS. WELL AND MASTER LOTO UPON ARRIVAL.
400757227Form 1712/1/201412/22/2014PLUNGER LIFT88GAS --10 WATER H20 898898No----"Surface casing produced 10 gallons of water during test. Monitored extra 30 minutes ended with 7 psi. Shut in surface casing For 15 minutes ended with 63 psi."