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Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-26518CLEMENT
32-11
PDC ENERGY INC
69175
SI
1/1/2025
WATTENBERG
90750
WELD  123
NWSW 11 4N66W 6
332590
   
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Surface Casing Depth: 529 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
404380427Form 179/18/202510/6/2025SHUT-IN29DOWN TO 0 GAS0 NO FLOW 980980No----Remediation follow up test. 29 PSI blew down to 0 PSI within first few seconds of test. No pressure or flow observed for the remainder of the test. Operator will monitor pressure and re-test according to bradenhead policy.
404082889Form 172/17/20252/5/2025SHUT-IN20CONTINUOUS WATER AND GAS20 CONTINUOUS 937937No----Annual Test. 20 PSI continuous water and gas, did not blow down, water and gas observed for entire test. PDC will schedule a sampling event and submit results via form 43. PDC will monitor pressure and re-test according to bradenhead policy.
403940733Form 179/30/202410/1/2024SHUT-IN27DOWN TO 0 GAS5 SURGE 910910No----Remediation follow up test. 27 PSI gas flow blew down to 0 PSI within first few seconds of test. No pressure or flow observed for 10 minutes when foamy liquid hydrocarbon surged and lasted for remainder of test. PDC will monitor pressure and re-test according to bradenhead policy.
403684476Form 172/9/20242/12/2024PLUNGER LIFT24DOWN TO 0 WATER AND GAS20 CONTINUOUS 00No----Annual test. 24 PSI water and gas flow blew down to 20 PSI in 30 minutes, ~15 gallons total fluid. PDC will monitor pressure and re-test according to bradenhead policy.
403550767Form 1710/4/202310/5/2023SHUT-IN24CONTINUOUS GAS0 CONTINUOUS 841841No----Abatement system follow up test. 24 PSI gas flow blew down to 0 PSI in 10 minutes. Water started 10 minutes after open and trickled for entire test, ~8 gallons fluid. PDC will continue to monitor monthly.
Click for SpecificsFull2/7/20233/15/2023 10Down to Zero--0No Flow780780NoNoneNone 
403020115Form 174/15/20224/19/2022SHUT-IN15CONTINUOUS WATER AND GAS20 CONTINUOUS 694694Yes----Annual Test, 15 PSI water and gas flow in the first five minutes, with water flow for the remainder of the test, increased to 20 PSI in 30 minutes. PDC will schedule a sampling event and submit results via form 43 as well as a remediation plan via sundry as soon as possible. PDC will continue to monitor monthly.
Click for SpecificsFull4/14/202111/1/2021 40Continuous--0No Flow327341NoNoneNone 
Click for SpecificsLight4/29/20205/11/2020 30 --30 ----NoNoNo 
401127788Form 175/19/201610/11/2016PLUNGER LIFT275GAS --0 WHISPER 303305No---- 
400404748Form 174/8/20134/16/2013PLUNGER LIFT240GAS --95 GAS 353358No----Surface casing produced no fluid during the form 17 test.