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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-24911ST. ACACIUS
18-35
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
8/26/2019
WATTENBERG
90750
MEAD/WELD  123
SWNW 35 3N68W 6
336490
   
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Surface Casing Depth: 860 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
402043177Form 174/30/20195/14/2019PLUNGER LIFT354GAS --1 GAS 758756Yes----Surface casing produced no fluid. Well shut in for 15min ended with 15psi. Surface casing blown down an extra 30min ended with a whisper. Tubing shut in.
400982587Form 174/14/20152/2/2016 159GAS --1 GAS ----No----POST REMEDIATION TEST. INITIAL POST REMEDIATION BLOW DOWN ON 4-9-15 STARTED WITH 18 BLEW DOWN TO ZERO PSI. CASING HAD A VACUUM BEFORE AND AFTER TEST. SC DID NOT PRODUCE ANY FLUID. 15 MIN BUILD UP, WHISPER. OPEN TO SALES, TEMP SHUT IN FOR HZ PREP AND SHUT IN UPON ARRIVAL.
400992095Form 179/30/20142/18/2016PLUNGER LIFT121GAS -->14 GAS ----No----CASING INACCESSIBLE---SC did not produce any fluid during test. Blew down extra 30 minutes ended with a whisper of gas. Shut in SC for 15 minutes pressure built up to 6 psi. Tubing and casing were closed and locked out.
400290206Form 174/19/20125/29/2012PLUNGER LIFT125GAS --25 GAS 311312No----No fluid was produced during 30 minute blow down