Skip to Main Content

Incident Search

 
BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-24714ROBERTS
35-15
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
2/24/2023
WATTENBERG
90750
WELD  123
NWNW 22 3N66W 6
336265
   
Search for Different Bradenhead:
County Code: Sequence Code:
 
Surface Casing Depth: 726 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
402728704Form 176/21/20216/24/2021 0NO FLOW NONE0 NO FLOW 00No---- Tubing Shut in. Surface Casing produced no liquid.
402512882Form 1710/12/202010/16/2020 1WHISPER --1 WHISPER 11No----Tubing Shut in. Surface Casing produced no liquid.
402438796Form 171/7/20207/7/2020 0NO FLOW --0 NO FLOW 00No----SURFACE CASING PRODUCED NO FLUIDS.
402232350Form 1711/2/201911/6/2019PLUNGER LIFT46WATER H20 --1 WHISPER 11No----Surface casing produced water. Tubing shut in.
402104758Form 176/18/20197/11/2019PLUNGER LIFT85WATER H20 --1 WHISPER ----No----SUrface casing producced water. 15 minute shut in resulted in 6 psi. Tubing and casing not built.
400982602Form 176/9/20152/2/2016 4GAS --1 GAS ----No----POST REMEDIATION TEST. SC DID NOT PRODUCE ANY FLUID. FRAC VALVE STABBED AND WELL TORN APART UPON ARRIVAL. 30 MIN BLOW DOWN, WHISPER. 15 MIN BUILD UP, 3. POST REMEDIATION BLOW DOWN ON 6-1-15 STARTED WITH 49 BLEW DOWN TO ZERO PSI.
400563771Form 171/20/20142/27/2014PLUNGER LIFT261GAS --64 GAS 745771No----SC PRODUCED NO FLUID.
400317277Form 177/31/20128/17/2012PLUNGER LIFT253GAS --127 GAS 508513No----No fluid was produced during form 17 test. No transducer to surface casing.