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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-24091WARDELL
29-29
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
9/12/2023
WATTENBERG
90750
WELD  123
SWSW 20 3N65W 6
336102
   
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Surface Casing Depth: 819 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
403402620Form 175/12/20235/15/2023 18CONTINUOUS GAS0 NO FLOW 15531553No----Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull3/16/20224/18/2022Plunger Lift14ContinuousNone--No Flow15081506NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull4/19/20215/17/2021Plunger Lift5ContinuousNone--No Flow14441444NoNoNo Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull1/31/20206/8/2020 39Continuous Flow 1Whisper (Very Low Flow)13091309NoNoNoTubing shut in. Surface casing produced no liquid.
Click for SpecificsFull12/10/201912/20/2019 27Gas--0Down To Zero13031303NoNoNoTubing shut in. Surface casing produced no liquids.
400835419Form 174/15/20155/5/2015PLUNGER LIFT185GAS --1 GAS 498498No----POST REMEDIATION: MONITORED THE SURFACE CASING AN EXTRA 30 MINUTES, PRESSURE STAYED AT A WHISPER. SHUT THE SURFACE CASING IN FOR 15 MINUTES, PRESSURE BUILT UP TO 4 PSI. POST REMEDIATION BLOW-DOWN ON 4-9-2015, PRESSURE WAS AT 175 PSI, AND BLEW-DOWN TO 0 PSI.
400289368Form 175/10/20125/25/2012PLUNGER LIFT397GAS --274 GAS 287300No----No fluid was produced during 30 minute blow down