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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-23968MCCORMICK
24-1
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
2/2/2023
WATTENBERG
90750
WELD  123
NESE 1 3N67W 6
332584
   
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Surface Casing Depth: 773 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
403220520Form 1711/1/202211/7/2022 2CONTINUOUS GAS0 NO FLOW 10321034No---- Tubing Shut in. Surface Casing produced no liquid.
403002801Form 174/1/20224/4/2022 0NO FLOW NONE0 NO FLOW 985985No----Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull10/11/202111/15/2021Plunger Lift0No FlowNone--No Flow948948NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull10/22/202012/21/2020Plunger Lift1WHISPER ----DOWN TO 0 836835NoNoNo Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull6/6/201912/10/2019 1Whisper (Very Low Flow) 0Down To Zero237246NoNoNoSurface casing produced no liquid.
401264450Form 173/15/20174/21/2017 1WHISPER --0 DOWN TO 0 624624No----SURFACE CSG PRODUCED NO FLUIDS. SHUT IN SURFACE CSG FOR 15 MIN.; ENDED WITH A WHISPER OF GAS.
400722408Form 179/16/201411/3/2014PLUNGER LIFT180CONTINUOUS --152 CONTINUOUS 487488No----SUARFACE CASING PRODUCED 20 GALLONS OF CONDENSATE ABORTED TEST IN 20 MINUTES DUE TO VOLUME OF CONDENSATE. AFTER A 15 MINUTE SHUT-IN SC PRESSURE WAS AT 168 PSI.
400366104Form 1711/21/20121/8/2013PLUNGER LIFT153CONTINUOUS --120 CONTINUOUS 317322No----Surface casing made 50 gallons of condensate. No transducer to surface casing.