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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-19929HSR MILLENSIFER FEDERAL
2-30A
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
6/7/2021
WATTENBERG
90750
WELD  123
NWNE 30 3N66W 6
330954
   
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Surface Casing Depth: 463 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
402577001Form 171/15/20211/18/2021 36CONTINUOUS GAS AND LIQUID HYDROCARBON1 WHISPER 549548No----Tubing Shut in. Surface Casing produced Liquid Hydrocarbon.
402477130Form 178/17/20208/28/2020 1WHISPER --0 NO FLOW 571572No---- Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull10/4/201912/20/2019 31Continuous Flow--1Whisper (Very Low Flow)561560NoNoNoTubing shut in. Surface casing produced condensate.
401052997Form 175/18/20165/24/2016 54GAS --10 CONTINUOUS 269270No----STOPPED TEST, SC PRODUCED 20 GALLONS OF CONDENSATE. SHUT IN SC FOR 15 MIN ENDED WITH 13 PSI.
400798981Form 172/6/20152/25/2015PLUNGER LIFT16CONTINUOUS --1 CONTINUOUS 405415No----SURFACE CASING PRODUCED 10 GALLONS OF CONDENSATE. 30 MINUTE BLOW-DOWN. 15 MINUTE BUILD-UP, 3.
400490369Form 179/27/201310/4/2013PLUNGER LIFT52WATER H20 --<1 GAS 472486No----SURFACE CASING PRODUCED 15 GALLONS OF WATER DURING TEST.