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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-103-10294ANT HILL UNIT
19-12
KT RESOURCES LLC
10775
SI
5/1/2023
WHITE RIVER
92800
RIO BLANCO  103
NENW 19 2N96W 6
316339
   
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Surface Casing Depth: 1117 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
403804945Form 175/23/20245/28/2024SHUT-IN59DOWN TO 0 VAPOR0 NO FLOW 640640No---- 
403763966Form 174/22/20244/22/2024SHUT-IN46NO FLOW NONE0 NO FLOW 620620No---- 
403441417Form 176/20/20236/21/2023SHUT-IN40DOWN TO 0 GAS0 NO FLOW 665665No---- 
403276676Form 1712/26/202212/31/2022SHUT-IN0NO FLOW NONE0 NO FLOW 720720No----This bradenhead test has indicated that there is no communication between the surface casing (8.625") and the 5.5" production casing. The lack of communication between casings and the fact that the production casing pressure did not change when the bradenhead was opened indicates that this well has pressure integrity in with the production casing. In my opinion this well protects the health, safety, welfare, the environment and wildlife resources in the environment. It is requested that this bradenhead test be accepted has an alternative MIT as it has shown wellbore integrity and KT Resources has been unable to contract a workover rig due to high demand of equipment in the current price environment. If approved, this well will be turned into line.