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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-103-06124GRAY
B-5
SCOUT ENERGY MANAGEMENT LLC
10779
IJ
4/1/2024
RANGELY
72370
RIO BLANCO  103
SWNW 18 2N102W 6
314559
   
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Surface Casing Depth: 743 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
Click for SpecificsFull8/12/20249/4/2024 345Continuous--0Whisper33NoNoNo 
Click for SpecificsFull8/14/20239/5/2023Injector370Continuous--0No Flow3030NoNoNo 
Click for SpecificsFull8/17/20229/6/2022Injection400Down to Zero--0No Flow00NoNoNo 
402788191Form 178/17/20218/23/2021INJECTION412CONTINUOUS GAS0 DOWN TO 0 7979No----Well has approved pressure management plan in place per Document # 402584723. We will continue to follow the approved plan to monitor and run diagnostics for the 1 year period ending on 1/27/2022.
402555979Form 1712/15/202012/17/2020INJECTION408CONTINUOUS GAS AND VAPOR0 WHISPER 1010YesYes-- 
402467866Form 177/30/20208/17/2020INJECTION200GAS --0 DOWN TO 0 139140No----COGCC FIELD INSPECTION REPORT 693802365 NOTED HIGH BRADENHEAD PRESSURE, AFTER INSPECTION IT WAS NOTED THERE WAS A BAD GAUGE; REPLACED GAUGE AND READINGS WERE NORMAL. DISCUSSED WITH CHUCK BROWNING COGCC INSPECTOR AND HE SUGGESTED TO SUBMIT FORM 17 AS DOCUMENTATION OF CORRECTED GAUGE READINGS.