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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-043-06182PATTI
32-29
INCREMENTAL OIL & GAS (FLORENCE) LLC
10417
PA
6/13/2023
FLORENCE-CANON CITY
24600
FREMONT  043
SWNE 29 19S69W 6
417781
   
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Surface Casing Depth: 720 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
403424380Form 176/5/20236/6/2023SHUT-IN0NO FLOW NONE0 NO FLOW 00No----This bradenhead test is being conducted prior to the planned plugging and abandonment of the Patti 32-29 well per COGCC COAs. This test has confirmed there is no communication between the surface casing or production string in the Patti 32-29 well. No tubing exists in the well and the 7" production string is still loaded with water from previous MIT tests. NOTE: The current -01 wellbore of the Patti 32-29 well is a failed side-track (2/27/13) that resulted in downhole directional tools stuck and abandoned after fishing attempts were unsuccessful. In 2015, a bridge plug was set at 1976' and capped with cement to 1980' and casing was filled with water and hydro-tested to 400 psi. Two successful MITs followed in 2016 (doc #401025705) and again in 2021 (doc #402879615). Operator finds no further opportunities available for this well and will proceed with plugging and abandonment to commence the next day.