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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-51813Drake
24N
PDC ENERGY INC
69175
PR
10/17/2024
WATTENBERG
90750
WELD  123
SWNW 17 4N64W 6
482390
   
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Surface Casing Depth: 1747 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
404218745Form 175/9/20255/27/2025FLOWING9DOWN TO 0 GAS0 NO FLOW 957957No----Remediation follow up test. 9 PSI blew down to 0 PSI within first few seconds of test. No pressure or flow observed for the remainder of the test. Operator will monitor pressure and re-test according to bradenhead policy.
403963768Form 1710/18/202410/21/2024FLOWING53CONTINUOUS WATER AND GAS1 WHISPER 32073205No----Post-Production test within 60 days of first sales. 53 PSI continuous whisper gas and slight fluid flow blew down to 1 PSI in thirty minutes, ~3.75 gallons fluid. PDC will collect a sample and submit results via form 43. PDC will monitor pressure and re-test according to bradenhead policy.
403701644Form 172/24/20242/28/2024SHUT-IN0NO FLOW --0 NO FLOW 00No----Initial Test Post Rig Release. 0 PSI, no pressure or flow observed for the entire 30 min test. PDC will monitor pressure and re-test according to bradenhead policy.