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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-48287Ottesen LE
06-351HNX
PDC ENERGY INC
69175
PR
1/1/2024
WATTENBERG
90750
WELD  123
NWSE 33 1N66W 6
449521
   
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Surface Casing Depth: 1862 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
Click for SpecificsFull11/20/202412/10/2024 17Continuous--0No Flow292291NoNoNoAnnual Test.  17 PSI blew down to 0 PSI within first few seconds of test.  No pressure or flow observed for the remainder of the test. PDC will monitor pressure and re-test according to bradenhead policy.
403620114Form 1712/6/202312/11/2023SHUT-IN16CONTINUOUS GAS0 NO FLOW 382382No----Annual Test. 16 PSI blew down to 0 PSI in 17 minutes. No pressure or flow observed for the remainder of the test. PDC will monitor pressure and re-test according to bradenhead policy.
Click for SpecificsFull11/23/202211/29/2022 24Continuous--0No Flow360355NoNoneNone 
Click for SpecificsLight8/27/20219/6/2021Plunger Lift21 --0 348345NoNoNoTest per NTO. Gas on open for 7 minutes and died. No flow for remainder of test.
402538012Form 1711/17/202011/23/2020PLUNGER LIFT38CONTINUOUS GAS0 NO FLOW 444444No----Test per 2020 NTO. Gas on open, died after 22 minutes. No flow for remainder of test.
402083947Form 176/14/20196/21/2019SHUT-IN32CONTINUOUS --0 NO FLOW 15311533YesYes--Test after DOFP. Continuous gas flow thru 1/4" needle valve until ten minute mark, down to whisper and eventually died. BH and production gas sample collected for isotopic analysis. At the time of this submission, 6/21/19 1:00PM MST, BH had only built back to 16 PSI.
401926135Form 171/26/20192/1/2019SHUT-IN0NO FLOW --0 NO FLOW 00No----Test prior to toe prep/frac.