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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-44520BUTTERBALL
12N-34HZ
KERR MCGEE OIL & GAS ONSHORE LP
47120
PR
3/25/2018
WATTENBERG
90750
WELD  123
NWNW 10 2N67W 6
330770
   
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Surface Casing Depth: 1869 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
Click for SpecificsFull7/12/20248/20/2024 1WhisperNone--No Flow276284NoNN Surface Casing produced no liquid.
Click for SpecificsFull8/23/20239/11/2023Plunger Lift1WhisperNone--No Flow264267NoNN Surface Casing produced no liquid.
Click for SpecificsFull10/7/202211/8/2022Plunger Lift2ContinuousNone--No Flow320320NoNN Surface Casing produced no liquid.
Click for SpecificsFull7/1/202112/21/2021Plunger Lift0No FlowNone--No Flow518518NoNN Surface Casing produced no liquid.
Click for SpecificsFull5/18/202011/2/2020 1Whisper (Very Low Flow) 0Down To Zero900900NoNoNo Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull11/25/201912/20/2019 1Gas--1Gas762803NoNoNoSurface casing produced no liquids.
401611226Form 174/12/20184/17/2018 1WHISPER --0 DOWN TO 0 24082408No----Surface casing produced no fluids. Surface casing shut in for 15 min ended with 0 PSI. Well and master shut in. Post turn on to sales form 17.
401513943Form 171/3/20181/15/2018 0DOWN TO 0 --0 DOWN TO 0 16181617No----Surface casing produced no fluids. Surface casing was dead at the start of the test. Drilled and uncompleted form 17.
401388155Form 178/24/20178/25/2017 0DOWN TO 0 --0 DOWN TO 0 ----No----PRODUCTION CASING WAS ON A VACUUM. SURFACE CASING PRODUCED NO FLUIDS. SURFACE CASING SHUT-IN FOR 15 MIN; ENDED WITH 0 PSI.