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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-44086Bunting
26P-302
PDC ENERGY INC
69175
PR
3/31/2019
WATTENBERG
90750
WELD  123
SWSE 26 5N65W 6
448963
   
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Surface Casing Depth: 1673 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
403877263Form 177/31/20248/5/2024PLUNGER LIFT52CONTINUOUS WATER AND GAS19 CONTINUOUS 420420No----Annual test. 52 PSI continuous gas and water flow blew down to 19 PSI in 30 minutes, ~5 gallons total fluid. PDC will monitor pressure and re-test according to bradenhead policy.
Click for SpecificsFull9/19/20239/25/2023Plunger Lift16Down to Zero--0Down to Zero342342NoNoNoAnnual Test. 16 PSI blew down to 0 PSI within first few seconds of test. No pressure or flow observed for the remainder of the test. PDC will monitor pressure and re-test according to bradenhead policy.
Click for SpecificsFull9/6/202210/10/2022 42Down to Zero--0No Flow364364NoNoneNone 
Click for SpecificsFull4/15/202111/1/2021 0No Flow--0No Flow531485NoNoneNone 
402447620Form 174/11/20207/21/2020 95WATER H20 --0 WATER H20 748746No----6 month follow-up test post abatement system install. PDC will continue to monitor pressure and report any increase in pressure to COGCC.
402031750Form 174/26/20195/3/2019FLOWING90DOWN TO 0 --0 NO FLOW 20132013No----Bradenhead test 90 PSI blew down to 0 PSI instantly. no flow or pressure for the duration of test. PDC will follow up iwth a sundry proposing a remediation plan
401612960Form 174/12/20184/18/2018SHUT-IN0NO FLOW --0 NO FLOW 00No----Post TD test no flow or pressure