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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-39197DOLPH
4N-1HZ
KERR MCGEE OIL & GAS ONSHORE LP
47120
PR
5/1/2023
WATTENBERG
90750
WELD  123
SESW 1 2N66W 6
419841
   
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Surface Casing Depth: 1210 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
Click for SpecificsFull6/18/20257/21/2025 27ContinuousNone0No Flow306306NoNN Surface Casing produced no liquid.
Click for SpecificsFull4/9/20245/6/2024 22ContinuousNone--No Flow425424NoNN Surface Casing produced no liquid.
Click for SpecificsFull1/24/20232/13/2023Plunger Lift49ContinuousNone--No Flow307304NoNN Surface Casing produced no liquid.
Click for SpecificsFull3/7/20224/18/2022Plunger Lift36ContinuousNone--Whisper351359NoNN Surface Casing produced no liquid.
Click for SpecificsFull3/4/20214/19/2021Plunger Lift40ContinuousNone--Whisper414417NoNoNo Surface Casing produced no liquid.
402521953Form 179/15/202010/29/2020 49CONTINUOUS --1 WHISPER 343323No----Surface Casing produced no liquid.
402437020Form 176/30/20207/2/2020 54CONTINUOUS --1 WHISPER 453456No----SURFACE CASING PRODUCED NO FLUIDS.
402134112Form 177/8/20198/5/2019PLUNGER LIFT161GAS --1 WHISPER 341337No----Surface casing produced no fluids. 15 minute shut in results in 31 psi. 30 minute blow down results in whisper.
400878585Form 177/23/20158/20/2015PLUNGER LIFT409GAS -->1 GAS 20112011No----DID NOT SHUT WELL IN DURING TEST. BLEW DOWN SURFACE CASING AN EXTRA 30 MINUTES ENDED WITH A WHISPER OF GAS. SHUT IN SURFACE CASING FOR 15 MINUTES PRESSURE BUILT UP TO 117 PSI. SURFACE CASING PRODUCED NO FLUIDS DURING TEST.