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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-38017PETTINGER
1N-18HZ
KERR MCGEE OIL & GAS ONSHORE LP
47120
PR
12/1/2025
WATTENBERG
90750
WELD  123
SWSE 18 1N65W 6
434202
   
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Surface Casing Depth: 1197 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
Click for SpecificsFull7/7/20258/11/2025 0No FlowNone0No Flow157157NoNN Surface Casing produced no liquid.
Click for SpecificsFull10/10/202411/12/2024 2ContinuousNone--No Flow123118NoNN Surface Casing produced no liquid.
Click for SpecificsFull11/27/202312/11/2023Plunger Lift1WhisperNone--No Flow265216NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull4/21/20225/16/2022Plunger Lift1WhisperNone--No Flow122122NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull5/10/20216/14/2021Plunger Lift1WhisperNone--No Flow146146NoNoNo Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull3/6/20206/8/2020 0Down To Zero 0Down To Zero200200NoNoNoSurface casing produced no liquid.
Click for SpecificsFull4/18/201912/10/2019 1Whisper (Very Low Flow) 0Down To Zero12381234NoNoNoTubing shut in. Surface casing produced no liquid.
400960562Form 1712/3/201512/28/2015 1GAS --0 DOWN TO 0 798785No----SC PRODUCED NO FLUIDS DURING TEST. SHUT IN SC FOR 15 MIN ENDED WITH ZERO PSI. DID NOT SHUT WELL IN DURING TEST.
400991065Form 176/30/20142/17/2016PLUNGER LIFT1GAS -->0 DOWN TO 0 ----No----CASING INACCESSIBLE---SC produced no fluid during form 17 test. Frac valves stabbed.