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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-33362PSC
13N-13HZ
KERR MCGEE OIL & GAS ONSHORE LP
47120
PR
1/1/2026
WATTENBERG
90750
WELD  123
SESE 13 3N68W 6
331619
   
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Surface Casing Depth: 919 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
404615033Form 174/7/20264/10/2026 52CONTINUOUS GAS1 WHISPER 520495No----ABATEMENT- Surface Casing produced no liquid.
404135358Form 173/19/20253/20/2025 24CONTINUOUS GAS0 NO FLOW 616618YesYesNoABATEMENT- Surface Casing produced no liquid.
403756209Form 174/15/20244/16/2024 29CONTINUOUS GAS0 NO FLOW 467483YesYesNoSurface Casing produced no liquid.
403385118Form 174/26/20234/26/2023 14CONTINUOUS GAS1 WHISPER 471483No----Surface Casing produced no liquid.
403035029Form 174/28/20225/2/2022 12CONTINUOUS GAS0 NO FLOW 489495YesYesNoSurface Casing produced no liquid.
402681777Form 175/4/20215/6/2021 10CONTINUOUS GAS1 WHISPER 488497YesYesNo Surface Casing produced no liquid.
402337604Form 173/10/20203/10/2020PLUNGER LIFT31GAS --1 WHISPER 517522No----SURFACE CASING PRODUCED NO FLUIDS.
402111402Form 176/20/20197/16/2019PLUNGER LIFT161GAS --109 GAS 678680YesYes--Surface casing produced no fluids. Surface casing blew down extra 30 minutes ended with a 75 PSI. Surface casing shut in for 15 minutes ended with 77 PSI.
402104089Form 176/20/20197/11/2019PLUNGER LIFT161GAS --109 GAS 678680No----surface casing produced no fluids. 15 minute shut in resulted in 77 psi. 30 minute blow down resulted in 75 psi.