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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-32991NICHOLS
22-8
KERR MCGEE OIL & GAS ONSHORE LP
47120
SI
7/1/2021
WATTENBERG
90750
WELD  123
NENW 8 2N65W 6
332301
   
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Surface Casing Depth: 841 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
Click for SpecificsFull3/17/20264/13/2026 1WhisperNone0No Flow12241224NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull4/29/20257/21/2025 1WhisperNone0No Flow12011204NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull2/6/20243/19/2024Plunger Lift0No FlowNone--No Flow11821182NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull6/12/20237/17/2023Plunger Lift0No FlowNone--No Flow11691169NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull3/25/20224/18/2022Plunger Lift0No FlowNone--No Flow11231123NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull4/15/20215/17/2021Plunger Lift1WhisperNone--No Flow10651065NoNoNo Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull2/11/20206/8/2020 10Continuous Flow 1Whisper (Very Low Flow)831835NoNoNoSurface casing produced no liquid.
402042923Form 174/30/20195/14/2019PLUNGER LIFT1GAS --0 DOWN TO 0 681710No----Surface casing produced no fluid. Well shut in for 15min ended with no psi.
400810187Form 173/5/20153/17/2015PLUNGER LIFT1GAS --0 DOWN TO 0 892895No----SURFACE CASING PRODUCED NO FLUIDS DURING TEST. SHUT-IN SURFACE CASING FOR 15 MINUTES, ENDED WITH 0 PSI. WELL WAS SHUT-IN FOR HZ PREP.