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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-30356SAWDEY
32-30
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
5/1/2024
WATTENBERG
90750
WELD  123
SENW 30 2N68W 6
323043
   
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Surface Casing Depth: 885 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
403679164Form 172/7/20242/7/2024 21CONTINUOUS GAS0 NO FLOW 20602057No----Tubing Shut in. Surface Casing produced no liquid.
403341714Form 173/7/20233/9/2023 20CONTINUOUS GAS1 WHISPER 21742176YesYesNoTubing Shut in. Surface Casing produced no liquid.
403286286Form 171/9/20231/11/2023 26CONTINUOUS GAS1 WHISPER 21782178No----Tubing Shut in. Surface Casing produced no liquid.
403180540Form 179/28/20229/28/2022 106CONTINUOUS GAS1 WHISPER 21702167No----Tubing Shut in. Surface Casing produced no liquid.
403030652Form 174/26/20224/28/2022 1WHISPER GAS0 NO FLOW 21572157No----Tubing Shut in. Surface Casing produced no liquid.
402962644Form 172/18/20222/22/2022 1WHISPER GAS0 NO FLOW 21362134No----Tubing Shut in. Surface Casing produced no liquid.
402904820Form 1712/20/202112/20/2021 23CONTINUOUS GAS0 NO FLOW 21362129No---- Tubing Shut in. Surface Casing produced no liquid.
402891087Form 1712/6/202112/7/2021 110CONTINUOUS GAS1 WHISPER 21682163YesYesNoTubing Shut in. Surface Casing produced no liquid.
402764619Form 177/22/20217/29/2021 85CONTINUOUS GAS1 WHISPER 21702170No----Surface Casing produced no liquid.
402441402Form 175/21/20207/10/2020 9CONTINUOUS --0 NO FLOW 22262236No----Surface Casing produced no liquid.
Click for SpecificsFull12/14/201912/20/2019 151Gas--22Gas22822280NoNoNoTubing shut in. Surface casing produced no liquids.
401060766Form 174/20/20166/9/2016 71GAS --1 GAS 836837No----SC DID NOT PRODUCED ANY FLUID. 30 MIN BLOWDOWN, WHISPER. 15 MIN BUILD UP, 3. INITIAL POST REMEDIATION ON 4-14-16 STARTED WITH 104 PSI AND BLEW DOWN TO A WHISPER.
400292309Form 174/24/20126/5/2012PLUNGER LIFT452GAS --268 GAS 492500No----No fluid was produced during 30 minute blow down