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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-29523NEWBY
19-33
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
3/7/2019
WATTENBERG
90750
WELD  123
SWSW 33 3N68W 6
336498
   
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Surface Casing Depth: 905 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
401837016Form 1711/5/201811/13/2018 114GAS --1 WHISPER 00No----SURFACE CASING PRODUCED NO FLUIDS. SURFACE CAING BLEW DOWN FOR AN EXTRA 30 MIN; ENDED WITH A WHISPER. SURFACE CASING SHUT-IN FOR 15 MIN; ENDED WITH 8 PSI. wELL AND MASTER VALVE SHUT-IN.
401780095Form 179/24/201810/1/2018 132GAS --1 WHISPER 00No----SURFACE CASING PRODUCED NO FLUIDS. EXTRA 30 MIN ENDED WITH WHISPER. SHUT IN 15 MIN ENDED WITH 8 PSI. MASTER SHUT IN.
401604792Form 173/26/20184/11/2018 190GAS --7 GAS ----YesYes--Surface casing produced no fluids. Blew down surface casing an extra 30 min ended with a whisper. Installed crystal gauge after blow down. Both tubing and casing were LOTO.
401192325Form 171/4/20171/24/2017 148GAS --8 GAS 390396No----SURFACE CASING PRODUCED NO FLUIDS. BLEW DOWN SURFACE CASING AN EXTRA 30 MIN, ENDED WITH A WHISPER. SHUT IN SURFACE CASING FOR 15 MIN, ENDED WITH 5 PSI.
400354547Form 1710/4/201212/5/2012PLUNGER LIFT74GAS --<1 GAS 373379No----No fluid was produced during form 17 test.