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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-29459SEC FOUR
12-4
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
5/10/2019
WATTENBERG
90750
ERIE/WELD  123
NESW 4 1N68W 6
336147
   
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Surface Casing Depth: 819 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
402060380Form 172/25/20195/31/2019PLUNGER LIFT25GAS --0  19671967No----Surface casing produced no fluid. Well shut in for 15min ended with a whisper. Tubing shut in.
401887462Form 1712/19/201812/27/2018PLUNGER LIFT29GAS --1 WHISPER 18261826No----Surface casing produced no fluids. Blew down surface casing an extra 30 minutes ended with a whisper. Surface casing shut in for 15 minutes ended with 6 PSI. Well and master valve were shut in.
401315637Form 176/8/20176/22/2017 1WHISPER --1 WHISPER ----No----SC PRODUCED NO FLUID DURING TEST. TUBING AND CASING WERE LOTO UPON ARRIVAL.
400828236Form 174/7/20154/21/2015PLUNGER LIFT23GAS --0 DOWN TO 0 733737No----POST REMEDIATION: BLEW-DOWN SURFACE CASING ON 4/2/15, STARTED WITH 28 PSI. SURFACE CASING PRODUCED NO FLUIDS DURING TEST. SHUT-IN SURFACE CASING FOR 15 MINUTES, ENDED WITH A WHISPER OF GAS.
400489458Form 179/5/201310/2/2013PLUNGER LIFT127GAS --2 GAS 701702No----SURFACE CASING PRODUCED NO FLUIDS DURING THE FORM 17 TEST.
400354765Form 1710/3/201212/6/2012PLUNGER LIFT112GAS --<1 GAS 652656No----No fluid was produced during form 17 test.