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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-27337SHABLE
24-20
NOBLE ENERGY INC
100322
PA
2/9/2022
WATTENBERG
90750
WELD  123
SENE 20 4N65W 6
332850
   
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Surface Casing Depth: 728 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
402863202Form 1711/4/202111/5/2021 85CONTINUOUS GAS0 NO FLOW 00YesYes--GAS PRESENT AT BEGINING OF TEST, GAS WAS NOT CONTINUOUS. BLEW DOWN TO ZERO, NO PSI LIGHT FLOW AT END OF TEST. NO TUBING OR PRODUCTION CSG.
402807414Form 179/9/20219/10/2021 26CONTINUOUS GAS0 NO FLOW 60No----GAS PRESENT AT BEGINING OF TEST, GAS WAS NOT CONTINUOUS. BLEW DOWN TO ZERO, NO PSI NO FLOW AT END OF TEST. NO TUBING. ENGINEERING REQUEST.
402628140Form 173/12/20213/15/2021 81CONTINUOUS GAS0 NO FLOW 00No----GAS PRESENT AT BEGINNING OF TEST. GAS WAS CONTINUOUS. GAS SAMPLE WAS COLLECTED.BLEWDOWN TO ZERO NO PSI NO FLOW AT END OF TEST
402508195Form 1710/8/202010/12/2020 158GAS --0 NO FLOW 2000YesYes--GAS PRESENT AT BEGINING OF TEST. GAS WAS NOT CONTINUOUS. GAS SAMPLE COLLECTED BLEWDOWN TO ZERO NO PSI NO FLOW AT END OF TEST. WELL WAS TREE'D DOWN. NO TUBING PRESSURE RECORDED. ANNUAL BLOW DOWN 2020
402363964Form 179/26/20194/7/2020 350GAS --0 NO FLOW 350350YesYes--OPENED SURFACE CASING TO TANK, DOWN TO WHISPER IN FIRST 5 MIN THEN NO FLOW/BLOW AFTER
402114823Form 177/17/20197/18/2019PLUNGER LIFT370GAS --0 WHISPER 330296No----GAS PRESENT AT BEGINNING OF TEST. BLEW DOWN TO 0. NO PSI NO FLOW AT END OF TEST. ANNUAL BLOW DOWN 2019.
400630074Form 176/3/20146/19/2014PLUNGER LIFT265CONTINUOUS --10 CONTINUOUS 636626No----oil gas surge continuous
400294944Form 176/5/20126/21/2012PLUNGER LIFT218GAS --120 CONTINUOUS 578578No----Surface casing produced 12 gallons of condensate during Form 17 test