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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-27093CARMA
13-25
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
7/13/2022
WATTENBERG
90750
FIRESTONE/WELD  123
NWSW 25 3N68W 6
336062
   
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Surface Casing Depth: 912 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
402659583Form 174/9/20214/15/2021 115CONTINUOUS GAS32 CONTINUOUS 99No---- Tubing Shut in. Surface Casing produced no liquid.
402504945Form 1710/5/202010/7/2020 127CONTINUOUS --1 CONTINUOUS 98No----Tubing Shut in. Surface Casing produced no liquid.
402131077Form 177/25/20198/1/2019PLUNGER LIFT144GAS --4 GAS ----No----Surface casing produced no fluids. 15 minute shut in results in 93 psi. 30 minute shut in results in 4 psi. Tubing and casing shut in.
402047292Form 175/6/20195/17/2019PLUNGER LIFT142GAS --67 GAS ----No----Surface casing produced no fluid. Well shut in for 15min ended with psi. Surface casing blown down an extra 30min ended with psi. Tubing shut in.
401960434Form 172/28/20193/5/2019PLUNGER LIFT142GAS --66 GAS ----No----Surface casing produced no fluid. Well shut in for 15min ended with pressure. Tubing and casing shut in for horizontal offset frac.
401604917Form 173/29/20184/11/2018 149GAS --51 GAS 2222YesYes--Surface casing produced no fluids. Blew down surface casing an extra 30 min ended with 39 PSI. Installed crystal gauge. Well and master shut in.
401092247Form 178/8/20168/11/2016 105GAS --25 GAS 66No----SC PRODUCED NO FLUIDS DURING TEST. BLEW DOWN SC AN EXTRA 30 MIN ENDED WITH 8 PSI. SHUT IN SC FOR 15 MIN ENDED WITH 48 PSI. WORKOVER VLAVE INSTALLED AND WELL SHUT IN
401075420Form 177/8/20167/8/2016PLUNGER LIFT137GAS -->27 GAS 00No----WORKOVER VALVE INSTALLED UPON ARRIVAL. SURFACE CASING PRODUCED NO FLUIDS DURING TEST. BLEW DOWN SURFACE CASING AN EXTRA 30 MIN. ENDED WITH 17 PSI. SHUT IN SURFACE CASING FOR 15 MIN. ENDED WITH 47 PSI.
400364728Form 1711/14/20121/4/2013PLUNGER LIFT48GAS --<1 GAS 473476No----Surface casing produced no fluid during the form 17 test.