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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-26902TALLGRASS
9-17
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
2/15/2019
WATTENBERG
90750
ERIE/WELD  123
SESE 17 1N68W 6
335564
   
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Surface Casing Depth: 974 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
401907696Form 171/14/20191/16/2019 13GAS --0 DOWN TO 0 13--No----SURFACE CASING PRODUCED NO FULIDS. SURFACE CASING SHUT-IN FOR 15 MIN; ENDED WITH 0 PSI.
401887535Form 1712/21/201812/27/2018PLUNGER LIFT29WATER H20 --1 WHISPER 301No----Surface casing produced water. Blew down surface casing an extra 30 minutes ended with a whisper. Surface casing shut in for 15 minutes ended with a whisper. Unable to guage tubing.
401780444Form 179/18/201810/1/2018 252GAS --1 WHISPER ----No----SURFACE CASING PRODUCED NO FLUIDS. SURFACE CASING SHUT IN FOR 15 MIN ENDED WITH 11 PSI. TUBING AND PRODUCTION CASING WERE LOTO.
401625983Form 174/16/20185/1/2018PLUNGER LIFT281GAS --1 WATER H20 ----YesYesYesSurface casing produced 7 gallons of water. Blew down surface casing an extra 30 minutes ended with a whisper. Surface casing shut in for 15 minutes ended with 12 PSI. Both tubing and casing were LOTO.
400766373Form 1711/17/20141/7/2015PLUNGER LIFT252GAS --51 WATER H20 511513No----SC PRODUCED 2O GALLONS OF WATER AND STOPPED TEST, SI SC FOR 15 MINS, ENDED WITH 88 PSI
400317532Form 178/10/20128/17/2012PLUNGER LIFT160GAS --<1 GAS 501506No----Surface casing produced no fluid during the form 17 test.