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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-26216DOUTHIT
10-26
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
5/26/2020
WATTENBERG
90750
MEAD/WELD  123
SWSE 26 3N68W 6
336167
   
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Surface Casing Depth: 780 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
402282340Form 171/9/20201/10/2020 73GAS --1 GAS ----YesYes--SURFACE CASING PRODUCED NO FLUIDS. TUBING AND PRODUCTION CASING LOTO.
Click for SpecificsFull9/12/201912/10/2019 71Gas 0Down To Zero00NoNoNoProduction casing and tubing shut in. Surface casing produced no liquid.
401290006Form 175/19/20175/23/2017 86GAS --1 WHISPER 116117YesYes--SURFACE CASING PRODUCED NO FLUIDS. BLEW DOWN SURFACE CASING AN EXTRA 30 MIN ENDED WITH A WHISPER. SHUT IN SURFACE CASING FOR 15 MIN ENDED WITH 3 PSI. WELL AND MASTER SHUT IN.
401076263Form 177/6/20167/11/2016 76GAS --1 GAS 240242No----SC PRODUCED NO FLUIDS DURING TEST . BLEW DOWN SC AN EXTRA 30 MIN ENDED WITH A WHISPER. SHUT IN SC FOR 15 MIN ENDED WITH 3 PSI. WELL AND MASTER SHUT IN UPON ARRIVAL.
400878404Form 177/7/20158/20/2015PLUNGER LIFT52GAS -->1 GAS 2120No----POST REMEDIATION TEST. SURFACE CASING DID NOT PRODUCE ANY FLUID. 30 MIN. BUILD-UP, 3. TEMP SHUT-IN FOR HZ PREP TORN APART UPON ARRIVAL. INITIAL POST REMEDIATION BLOW DOWN ON 6/29/2015 STARTED WITH 76 PSI AND BLEW DOWN TO 0 PSI.
400352984Form 1710/16/201212/3/2012PLUNGER LIFT34GAS --<1 GAS 370387No----No fluid was produced during form 17 test.