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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-25666CANNON
15-11
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
5/5/2021
WATTENBERG
90750
WELD  123
SWSE 11 2N66W 6
309974
   
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Surface Casing Depth: 1036 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
402564170Form 1712/30/202012/31/2020 239CONTINUOUS GAS133 CONTINUOUS 892902No----Tubing Shut in. Surface Casing produced no liquid.
402536994Form 1710/2/202011/20/2020 295CONTINUOUS GAS113 CONTINUOUS 877877No----Tubing Shut in. Surface Casing produced no liquid.
402021214Form 174/23/20194/25/2019PLUNGER LIFT363GAS --239 GAS 460458No----Surface casing produced no fluid. Well shut in for 15min ended with psi. Surface casing blown down an extra 30min ended with psi
401586515Form 173/15/20183/26/2018 508GAS --440 GAS 882882YesYes--Surface casing produced no fluids. Surface casing shut in for 15 min ended with 445 PSI. Well and master shut in.
401466436Form 1711/14/201711/21/2017 650GAS --483 GAS 871875No----SURFACE CASING PRODUCED NO FLUIDS. SURFACE CASING BLOWN DOWN FOR EXTRA 30 MIN ENDED WITH 497 PSI. SURFACE CASING SHUT IN FOR 15 MIN ENDED WITH 499 PSI. MASTER VALVE WAS SHUT.
401361642Form 177/19/20178/1/2017 554GAS --465 GAS 750750No----MASTER VALVE WAS SHUT. SURFACE CASING PRODUCED NO FLUIDS. SURFACE CASING BLOWN DOWN EXTRA 30 MIN ENDED WITH 380 PSI OF GAS. SURFACE CASING SHUT IN FOR 15 MIN ENDED WITH 381 PSI OF GAS.
401054396Form 175/24/20165/26/2016 520GAS --430 GAS 378393No----SC PRODUCED NO FLUIDS DURING TEST. BLEW DOWN SC AN EXTRA 30 MIN ENDED WITH 367 PSI. SHUT IN SC FOR 15 MIN ENDED WITH 375 PSI.