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BradenheadView Related Related View DocsDoc
 
Facility TypeFacility ID/
API
Facility Name/
Number
Operator Name/
Number
StatusField Name/
Number
LocationLocation ID
WELL05-123-25262USA
19-36
KERR MCGEE OIL & GAS ONSHORE LP
47120
PA
7/7/2022
WATTENBERG
90750
WELD  123
SESW 36 3N66W 6
309697
   
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Surface Casing Depth: 906 ft.
View Form/DetailsReport TypeTest DateSubmit DateWell StatusInitial Surf CasingBradenhead Flow (Start)Fluid TypeEnd Surf CasingBradenhead Flow (End)Initial Prod CasingEnd Prod CasingSample Taken?GasLiquidComments
403000329Form 173/31/20223/31/2022 2CONTINUOUS GAS0 NO FLOW 565564No----Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull1/27/20222/21/2022Plunger Lift2ContinuousNone--No Flow545544NoNN Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull2/17/20213/15/2021Plunger Lift2ContinuousNone--No Flow395396NoNoNo Tubing Shut in. Surface Casing produced no liquid.
Click for SpecificsFull1/21/20206/8/2020 1Whisper (Very Low Flow) 0Down To Zero385385NoNoNoTubing shut in. Surface casing produced no liquid.
Click for SpecificsFull2/13/201912/10/2019 1Whisper (Very Low Flow) 0Down To Zero622622NoNoNoTubing shut in. Surface casing produced no liquid.
400828953Form 174/15/20154/22/2015PLUNGER LIFT1GAS --0 DOWN TO 0 954953No----POST REMEDIATION: AFTER 15 MINUTE SHUT-IN, SURFACE CASING STAYED AT 0 PSI. POST REMEDIATION TEST ON 4-9-2015, PRESSURE WAS AT A WHISPER AND BLEW-DOWN TO 0 PSI.
400292302Form 174/18/20126/5/2012PLUNGER LIFT471GAS --424 GAS 363395No----No fluid was produced during 30 minute blow down